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October 27, 2024

PJM Market Implementation Committee

© RTO Insider LLC
PJM: ‘Conservative Operations’ Maintained Reliability During Jan. 2024 Storm
PJM spent $53.5 million on conservative, out-of-market dispatch procedures to maintain reliability during the January 2024 Winter Storm Gerri.
© RTO Insider LLC
PJM MIC Briefs: Feb. 7, 2024
The PJM Market Implementation Committee endorsed manual revisions codifying the real-time temporary exceptions process for generators to report any issues that may prevent them from operating to their unit-specific parameters.
PJM
PJM MIC Briefs: Jan. 10, 2024
The Market Implementation Committee discussed PJM's analysis of how proposed Critical Issue Fast Path filings before FERC might have impacted the 2024/25 Base Residual Auction results.
PJM
PJM MIC Briefs: Dec. 6, 2023
PJM’s MIC heard updates on capacity market proposals pending before FERC and began a review of how energy efficiency resources participate in the market.
PJM
PJM MIC Briefs: Aug. 9, 2023
PJM's Market Implementation Committee endorsed one of several packages to create new rules for generators with co-located load and rejected four proposals revising how generators providing reactive power service are compensated.
PJM
PJM MIC Briefs: Dec. 7, 2022
A poll by the Market Implementation Committee found little support for two competing proposals on capacity offer opportunities for co-located load.

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